孤东油田七区西聚合物驱示踪剂井间监测及油藏调整矿场试验研究 / Polymer Injection Tracer Test and Adjust Developraent Project Experimental Study East of Region 7 in Gudong Oilfield
- Resource Type
- Academic Journal
- Authors
- 姜颜波; 江小芳; 赵伟; JIANG Yanbo; Jiang Xiaofang; Zhao Wei
- Source
- 油气井测试 / WELL TESTING. 10(1):63-66
- Subject
- 注聚合物
示踪剂
动态监测
试验
堵水
polymer waterflooding
tracer
performance monitoring
testing
water shut off
- Language
- Chinese
- ISSN
- 1004-4388
经对孤东油田七区西Ng52+3层聚合物驱工业性矿场试验过程中油水井间大孔道窜流的 实际情况进行分析,探讨了化学示踪剂井间监测的机理;根据监测结果,讨论了油水井间的连通状 况,实施了堵水调剖油藏调整。这项研究对于注聚区整体堵水调剖,扼制聚合物溶液窜流,扩大波 及体积发挥了重大作用。
After analyzing the cross flow in the large pore in the Ng52 + 3 formation in the west of Region 7 in Gudong oilfield, the chemical tracer test mechanics is discussed, and the field experiment is performed. According to the tracer test results, the connectivity between the wells are discussed. The reservoir development project adjustment has got benefit. The whole reservoir development project adjustment limits the cross flow and extend the swept volume.